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Prop story

Fri Mar 02, 2007 1:08 pm

Reading the site about Gary doing maintenace on Eric's Skyraider and pulling the prop, reminded me of another prop story from Breckenridge. I though Gary might pick up on it, but it was probably before his time there. Anyway, well known Warbird pilot Howard Pardue, had a small replica homebuilt, I think it was a FW 190. One day he was flying along nice and steady, day dreaming of future obscene oil profits, when something flying out in front of the nose caught his eye. The next thing he noticed was how smooth the engine was even though it was revving up high. Next he noticed he wasn't getting much thrust although the engine was making good power. It dawned on him that he had a runaway prop problem; or to be more accurate a flyaway prop problem, that had nothing to do with the govenor, but everything to do with the prop. He glided down to a sucessfull forced landing, and later the prop was found unharmed in a field. Lest one think this is only a good story, it was told to me by Howard himself, and would a Marine lie? Also, I have seen the prop on his wall, it was a black wooden fixed pitch four bladed one, and pretty neat looking handiwork. The story did not include any info about who had last secured or not secured the prop, and it may be too late to analzye the fingerprints on it to compare with the usual suspects.

Fri Mar 02, 2007 1:39 pm

HOLY CRAP :shock: And I thought stalls would be scary. :roll:

Mudge the amazed

Fri Mar 02, 2007 1:52 pm

Interesting story Bill.

Sounds just like a little incident my brother had. Wooden props are great, just need to check the torque ALOT. Weather changes can make the wood strink and swell.

Accident report (Note: my brother called this the accident that wouldn't stop):

On December 12, 1999, at 1750 central standard time, a King Lancair 235/320 amateur-built experimental airplane, N717SK, owned and operated by the pilot, was substantially damaged during a forced landing following the separation of the propeller near Sterling City, Texas. The instrument rated private pilot, sole occupant of the airplane, was not injured. Visual meteorological conditions prevailed, and an IFR flight plan was filed for the 14 Code of Federal Regulations Part 91 personal flight. The IFR cross-country flight originated from Kerrville, Texas, at 1622, with Big Spring, Texas, as its destination.

The pilot reported that while at 10,000 feet msl and 70 miles from Big Spring, Texas, Fort Worth Center cleared him to descend at "pilots discretion to 4,600 feet." During the descent, at 6,500 feet, he heard a noise that sounded like a "magneto dropping out or a gear door coming open. There was no noticeable vibration in excess of the normal engine effects." He reduced power to 1,400 rpm and checked the magnetos and hydraulic system. All systems were "fine." The pilot further reported that one minute prior to hearing the noise, he detected a "smell like something was hot or burning. Nothing was apparent by visual observation. Thirty seconds after the noise began the sound ended abruptly. The only sound that you could hear then was the engine running extremely smooth." He looked at the tachometer and it was indicating 3,000 rpm. He reduced the power to 2,400 rpm and "realized that the propeller may have come off." He reported the problem to Fort Worth Center, and was advised of several nearby airports and ranch airstrips; however, he was unable to reach them.

The pilot stated that he turned to the northeast to look for a road to land on. He selected a county road, and during the approach, the aircraft's left main landing gear "stuck the bottom wire of a two wire service line" which crossed over the road. The airplane "stalled," yawed 20 degrees to the left, and "hit the middle of the road on all three [landing] gear." It then headed off the left shoulder of the road where the right wing hit a road sign, shearing off the outboard 4 feet of the wing. The airplane continued into an area between the road and a fence. As it crossed over a "road crossing" all landing gear were sheared off. The aircraft came to a stop upright 600 feet from where it had touched down on the road. The propeller assembly was not recovered.

The pilot reported that the Bruce Tiff/Collin Walker, 3-bladed wooden experimental propeller had accumulated 47.4 hours since installation.

Portions of four of the six propeller attaching bolts were removed from the engine and sent to the NTSB Materials Laboratory in Washington D.C., for examination. The examination revealed that all four bolts separated on relatively flat transverse planes. Examination of the fracture faces at low magnifications with the aid of a bench binocular microscope and then at higher magnifications with a scanning electron microscope (SEM) revealed ratchet marks and crack arrest positions. Both the fracture topography and fracture surface markings were typical of fatigue cracking. The shank of one of the bolts, in the area located immediately adjacent to the fracture face, had been subjected to "extensive rubbing damage." Two of the submitted bolt pieces contained washers. Examination showed that both washers were permanently deformed into dish shapes and were galled by rubbing. Rubbing and galling damage was also found on contact surfaces of the self locking nuts on all four bolts.

Fri Mar 02, 2007 2:06 pm

Interesting stories y'all.

And Bill, that was indeed before my time at BKD. Hadn't heard that one before.

Gary
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