marine air wrote:
So, it seems there are a couple trains of thought on this. What was going on inside the engines, how were they being operated , maintained , and operated. The number four engine may have been fine and airworthy but wS out of tune, especially the magnetos and the fine tuning of this part of the system. It’s not like it blew a piston or other catastrophic failure.
The umber 3 engine. It needs to be discerned what was going on with this engine and prop. Let’s hope they didn’t feather and shut down the wrong engine. Worse would be a prop that wouldn’t feather correctly or come out of feather. Yes, I’ve heard of pilots continuing to fly airplanes that needed work and the prop feathering equipment was faulty. That’s on the before takeoff checklist on the King Air, etc.
There’s no evidence the number 4 engine was failing . There’s evidence it’s rigged electrical system was in failure. One question I have about the spark plugs being fouled out; is it possible that they were being cleaned at regular intervals but the engines were being run too rich , say full rich even at cruise , and this practice caused them to be loading up? Last, are we concluding that the aircraft commander wS also the aircraft manager, dispatcher, and chief mechanic on the airplane? That’s an incredible workload for one person, especially a 77 year old. Please clarify.
First of all, hello everyone! I am new to the forum, it's been very educational reading through this thread and others... truly a great repository of knowledge here.
So to discuss the results of the report as they are relevant to this response, it's probably best to talk about what the ignition system issues identified with the No. 4 engine mean. There's talk of a "tuning issue." When we speak of tuning issues, we're talking about issues with the ignition timing, and the ignition system is assumed to be fully functional. "Tuning issues," while mechanically minor, can actually cause an engine to be inoperable, as anybody who has tried to rebuild a distributor can attest. What was going on with the No. 4 engine, according to the FAA, was NOT a tuning issue. To say that "the No. 4 engine was not failing, its electrical system was" is missing the point entirely: for the engine to have a hope of running, it needs fuel, air, and spark. So, from that standpoint, the No. 4 engine was not airworthy.
As for the No. 3 engine, others have pointed out that the spark plug problems could have been caused by a variety of reasons. Whatever the reason, they remain just that: Spark Plug Problems. Crud on the plugs points to poor operation/output of the engine caused by cold, rich running for a long period. The phrase "Italian Tune-Up" describes thrashing an engine to remove these kinds of carbon deposits from the plugs, as would be found on an engine that has been run conservatively for a long period. Think of a grandma taking an otherwise-mint Rambler down the block to church every Sunday- the engine never gets warm, the choke is never used, ect. The gaps being out-of-spec would have compounded the ignition problems experienced by the No. 3 engine. For an engine to run right, the spark has to happen strongly and reliably at the correct time. Gunked-up plugs will prevent this from happening, and as a result, could fire unpredictably or not at all, resulting in the detonation seen during the teardown.
So, having discussed briefly the implications of the FAA's findings, it brings us to the point- how did these problems cause the airplane to crash? That has more to do with the human side of the operation than the mechanical side. That's actually the implicit conclusion of the FAA's rescission. Witnesses reported that there were issues starting the No. 4 engine before the fatal flight. The pilot, who was also responsible for the maintenance of the aircraft, mis-diagnosed the terminal ignition system failure of the No. 4 engine as condensation in the magnetos. While vapor condensation can cause a magneto to fail to produce a reliable spark, the inspection completed by the engine shop showed that this was not the cause of the No. 4 engine's ignition system failure. The pilot thought that in order for the No. 4 engine to be operable, it required the magnetos to be "blown out," or cleared of water- in reality, the entire ignition system required an overhaul.
As for the No. 3 engine, the spark plug issues lead to a family of possible conclusions, none of which are compatible with safe operation of the aircraft. Almost certainly, the poor condition of the spark plugs can be directly attributed to a chronic lack of maintenance. Discounting the proximal causes of the spark plug fouling and damage, the fouled and damaged plugs would only have been present if they hadn't been repaired or replaced, as would have been the case if the engine were being competently maintained. It is difficult to pinpoint those proximal causes- however, the most likely explanation is that the spark plugs became damaged due to the engine being operated continuously at the lower edge of its performance envelope. The R-1820 was never designed to be babied around. It (the -97 version) was designed to run heavily boosted, with very high-octane fuel. Similarly, the airframe was designed and tested around engines that were producing 1200 horsepower. Deviate from that design intent for a long period of time, and you enter the world of "results not guaranteed."
None of the issues identified in the FAA's report would have caused a fatal accident on their own. However, their rescission of the Colling's Foundation's exemption points to a foregone conclusion: that the manner in which the aircraft was operated and maintained (somehow by the same person) 1) caused the subsystem failures and 2) contributed directly to the fatal crash. The report does not fully identify the causes of the accident, however it establishes sufficient reason to place responsibility for these contributing factors directly on the operating organization. In other words, if there is a way to safely operate warbirds for display or ride-along flights, this wasn't it.
This was an extremely tragic event. I have many fond memories of seeing Nine-O-Nine at our local airfield, including a couple of times with my late Grandfather- a combat-veteran B-17 pilot. It makes me extremely sad to realize that this crash could jeopardize continuing that experience for future generations, and their connection to a heroic past. Hopefully, there can be a silver lining from this accident and subsequent investigation: that lessons will be learned, and pave the way to safer continued operation of these historic machines.